05stroker
Never enough power guy!
Don't know yet. I do know the regulator never made up for the boost on the last pull. The WG didnt open either. I hit 19 psi with about 16 psi FP IIRC. Something happened and the regulator never made up for the boost. These road pulls leave very limited time for watching the gauges at these levels. I am on my way to get it back together though. I will not be able to do back to back results on the Comp 127550 cams vrs my custom grinds though, since I am installing them now with the new springs. I have to have a new #8 sleeve and piston, along with new rings and bearings since the metal got to the bearings. I have some diagnosis to do on the fuel system to see what actually caused this though.
Let me stress that this is NOT a tuning issue. I was dataloging when it happened. The fuel system never made up for the boost on the pull. This is a mech. failure of some sort. I just need to figure out what it was before I proceed.
I still think it has to be a leak somewhere, lines or even the regulator membrane itself, what makes me think that way is how it occurred when boost raised rapidly, after transmission shifted and raise rate was lower everything went back to normal and fuel pressure was back there.
Either way, redesigning the layout will only help.
This is the issue that we are looking into, while in fast RPM raise, regulator lost fuel control and did not compensate, once it shifted it recovered control.
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Any help guys? I am open to suggestions...
I will not exclude any thing at this point. The new parts are all almost here and I still dont know 100% what happened.
Can fuel or oil puddle and the intake and cause something like this?
EDIT: All vac lines came off the bottom of the JPC intake.
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