Well I'm Officially F@CKED!
As you guys know I took my car to another tuner 3 weeks ago and he saw and fixed issues with too much fuel being added(From SpeedFreaks) also it didnt make anywhere the hp I was told. During that time I had the p151a error and tried to fix that. I replaced all the plugs and re-gapped to .028 also replaced 2 O2 sensors(but none of that helped). The new tuner told me its not the intake runners but Ford and you guys told me it was. A week later I find out about the 2 missing bolts holding the collector on and get that fixed( fixing a big ehaust leak). I heard about another tuner that was closer to me (Sac-town) and read some good things so I decided to have him take a look. The tuner did a leak down and compression check before tuning today and this is what he saw..
Leak Down: test with 99psi
Cylinder:
#1 = 6%
#2 = 7%
#3 = 6%
#4 = 6%
#5 = 15%
#6 = 17%
#7 = 10%
#8 = 18%
Compression:
#1 = 215
#2 = 205
#3 = 210
#4 = 210
#5 = 180
#6 = 180
#7 = 190
#8 = 175
Also, #5, 6, 8 Plugs were toast (after 2 weeks!). All I can guess is that
1.) Tuner in Tracy forgot bolts or didn't tighten down pipe bolts and tuned over it by injecting more fuel and maybe more timing. In a way I think it covered the problem (sort term)
2.) months go by ( I dont dive the car all the time) and things get worse ( cant start engine without stepping on the gas and big puff of unburnt smoke)
3.) Checked plugs and see some of them messed up (later replaced them)
4) had hope of saving the car and took it to another tuner that saw and fixed the start up issue and saw the mass amount of gas being tuned in. Tuner saw an issue at 4.5K but didnt know what it was and thought it could be the plug gap(aka spark blow out. At the time I gapped them to .030).
5) I re-gapped the plugs to .028 ( pushing 12+psi). With the new tune the car started up with no puff of gas, but now has p151a error.
6) With in 2 weeks I replaced 2 O2 sensors and took it to ford (The told me its intake runner code).
7) Next day We spot the exhaust leak( no bolts on Down pipe on passenger side).
8) Day after that took it to midas to bolt it back up (PITA to do from home).
9) Now with Exhaust leak fixed, noticed more back fire and narrow band gauge (I know it sux) read lean at start up and hit low a few times.
10. Since the exhaust leak fix I have drove it for maybe 100 miles and shifted at 3K. I needed to get it tuned again and took it to ANOTHER tuner in Sac and now I hear this. Can All this hell really have been a stupid exhaust leak not noticed by 2 tuners? Does this make since? I'm stuck now and it does look like more $$.

I just cant believe this shit is happening to me again. tomorrow, I will meet the tuner and get the 3 plugs. I will most likely have him do everything as I'm F'ed up with all this